Posts
221
Joined
9/17/2010
Location
Oakbank,Mb, CA
Edited Date/Time
8/12/2016 3:47pm
hey guys,
a few weeks ago i finally got my 87 out. she ran amazing for about 4 laps then something strange happened.
in a corner she went wide open and the kill switch wouldn't work, so i pulled the plug cap and it didn't shut down. i had to shut off the fuel and lay it over.
it was running really hot, i put engine ice in her and probably half of it boiled out.
the main jet is a 162, im running a pro-circuit works pipe, our elevation is 785ft, and average riding temperature is between 77 and 86 Fahrenheit.
i did a leak down test and the only leaks i could find were at both of the top power valve covers. the throttle tube was a bit on the sticky side , but the slide appeared to be working fine. the idle knob had to be turned way up to get her to idle a bit, almost like the choke is half way up.
any ideas? the other PJ carb i have has a 180 main jet in it.



a few weeks ago i finally got my 87 out. she ran amazing for about 4 laps then something strange happened.
in a corner she went wide open and the kill switch wouldn't work, so i pulled the plug cap and it didn't shut down. i had to shut off the fuel and lay it over.
it was running really hot, i put engine ice in her and probably half of it boiled out.
the main jet is a 162, im running a pro-circuit works pipe, our elevation is 785ft, and average riding temperature is between 77 and 86 Fahrenheit.
i did a leak down test and the only leaks i could find were at both of the top power valve covers. the throttle tube was a bit on the sticky side , but the slide appeared to be working fine. the idle knob had to be turned way up to get her to idle a bit, almost like the choke is half way up.
any ideas? the other PJ carb i have has a 180 main jet in it.




Had it happen with 1979 Rocket motor, it was sucking the base gasket in on one side. (The top face of the LH crank case was bent slightly from a previous owner/builder being a ham fisted idiot!!) It would run perfectly for a lap or so, then as it got hot everything expanded a little, and it would suck the base gasket in and it would stick wide open.
When they suck air they can run REALLY hot, really fast as all the extra air leans them out. The extra heat could cause it to pre-ignite, that might be why pulling the plug cap didnt' do anything.
Stevie
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Engine runaway is when the motor revs up freely on it's own. Preignition is taking place in which no spark is needed. A red spark plug or piece of glowing carbon pre-ignites the fuel mixture and causes engine to continue picking up speed until failure. That's why the kill switch and removing the plug cap does not shut it off.
Causes
In order for this to happen, there has to be a lean condition present. Any kind of air leak could potentially lead to destruction. Intake gaskets, carb gaskets and crank seals seem to be common culprits.
I had this happen once when I turned the fuel off to run the fuel out of the bowl, which was the cause of the lean condition.
Check your throttle cable where it enters the carb cap. A good tip is to safety wire the cable down. It can pull up and sit on top of the brass fitting.
Pit Row
Your issue with the varying thickness of head gaskets is something to be careful of. Most generic gasket sets come listed 86-91 or 89-91 or some variation on the years. These usually come with a very thin (0.25mm) metal head gasket which is not correct for the early 87/87's.
If you look at the cylinder head of the 86/87's, the combustion chamber isn't very deep, in fact it looks like the head has been skimmed! The later models, the chamber is machined deeper with very distinct "lip" around the edge.
The '86-'87's used a thicker head gasket. (it's either 1mm or .75mm. I can't find my old one to measure up!) which is still available from Honda, part #12254-KS7-881. The original was fiber with a metal inner ring, the newer version is a multi layer metal type.
It sounds like your motor has had the later thin head gasket fitted, which not only causes sealing issues (I imagine an epoxied in stud wouldn't help with that either!!) it also can cause detonation as it basically drops 0.5-0.75mm off the cylinder head!!
Stevie
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