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76 to 82 Yamaha YZ125 stock 56mm piston - piston to cylinder clearence if .005"
Yz125 Piston with SKF HK1616 bearing with some spacers - the bearing had to be pressed in to the connecting rod, The spacers were something to make sure the bearing wasn't going to walk ut of the rod
The bearing installed in the rod.
This picture is not with piston at top dead center, flywheel magnets kept pulling it down.
The Shop
I was wrapping my head around how'd I'd do my MX6 125. I think I'd use a degree wheel align a pointer to the degree wheel and one to rotor,, and then rotate 8* and mark the rotor. This could be done on a lathe or even a drill press if it makes it easier to see than on bike.
I may have skinned the wrist pin bearing differently,,,bushed the small end with a bronze or steel bushing like done on a typical race car connecting rod. Not sure how the needles against a bronze bushing would fair,,so steel maybe needed.
I really dig your problem solving creativity....most people just give up and push the bike in corner and say I can't find parts for it...like in the great American "Larry the cable guy" Get er done!
As far as installing the bearing,which was a little tighter than I thought it would be. I made a puller from a 8mm bolt, nut & washers with a appropriate sized sleeve. The bearing was a little wider than the rod, I wish it were a little wider, but the 22mm wide bearing was too wide for the piston.
I actually heated the cyl & froze the sleeve and reinstalled it. I turned it about 1.5mm so as to work better with the YZ125 piston to turn the edge of a port a little farther from the ring end gap.
To get the cylinder liner out i got a tin/steel can that was deeper than the total height of the cylinder and was about 2x the diameter than the cylinder liner. With the cylinder assy upside down on the tin can(used the can to catch the liner in case it dropped out on its own.) Put it into the oven(told my wife it might sell a bit but I'd turn one the vent fan. She was ok with that.) and turned the oven up to 450f. after 30min, it didnt drop out on its own so I took it out and with it upside down still & lightly pushed with a wide flat blade screw driver where the rear transfer port is(you can see from the picture the sleeve is well exposed there as the port is just a big hollow area to the top of the port). The sleeve pushed easily pushed out about 1/2 way. I put it back in the oven for about 10 min and took it out with hot mitts and the sleeve easily pulled right out.
When I reinstalled the sleeve, I froze the liner over night in the freezer and put the cylinder in the oven at 450f again for approx 30 min. I pushed the sleeve about 90% of the way in(it would have gone all the way but i wanted it close so I could turn to line up the alignment marks that i scribed into the aluminum cylinder). I put it back into the oven for 10 min and then turned the liner to the appropriate mark and then pushed it down hard and fast(felt it "slam" and seat against the aluminum cylinder). It didnt drop out as nicely & freely as most Rotax cylinders I've done before but it didn't fight at all and is an easy job.
Finally done.......almost a year and a 1/2. Im very happy with the way it turned out though I dont know what the long term durability of my modified wrist pin bearing, guess it cant do any worse than fail. I think the only thing left will be to maybe some color matching numbers(blue, orange, black....something like that). But, I guess its ready for Unidilla Rewind 2018. Its been a fun project, but theres also been some major headaches. My next project is a 94 ATK 250.......next winter project!! Thanks everyone for all the help along the way and I hope i was able to help someone else.
Pit Row
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